summaryrefslogtreecommitdiffstats
path: root/board
diff options
context:
space:
mode:
authorSimon Glass <sjg@chromium.org>2011-11-05 04:46:51 +0000
committerAlbert ARIBAUD <albert.u.boot@aribaud.net>2011-12-24 10:23:31 +0100
commita04eba99f5a00aff54bef32cafa986830b094532 (patch)
tree22aac2fe25a1a1775b4828f65bae2d8958e0304f /board
parent4560c7decc1b13121072621cee9874e042c059b7 (diff)
downloadblackbird-obmc-uboot-a04eba99f5a00aff54bef32cafa986830b094532.tar.gz
blackbird-obmc-uboot-a04eba99f5a00aff54bef32cafa986830b094532.zip
tegra2: Plumb in SPI/UART switch code
On Seaboard the UART and SPI interfere with each other. This causes the UART to receive spurious zero bytes after SPI transactions and also means that SPI can corrupt a few output characters when it starts up if they are still in the UART buffer. This updates the board to use the SPI/UART switch to avoid the problem. For now this feature is turned off since it needs changes to the NS16550 UART to operate. Signed-off-by: Simon Glass <sjg@chromium.org> Signed-off-by: Tom Warren <twarren@nvidia.com>
Diffstat (limited to 'board')
-rw-r--r--board/nvidia/common/board.c8
-rw-r--r--board/nvidia/common/board.h1
-rw-r--r--board/nvidia/seaboard/seaboard.c3
3 files changed, 12 insertions, 0 deletions
diff --git a/board/nvidia/common/board.c b/board/nvidia/common/board.c
index 6a1312c5aa..c3f6796d5d 100644
--- a/board/nvidia/common/board.c
+++ b/board/nvidia/common/board.c
@@ -112,9 +112,13 @@ static void pin_mux_uart(int uart_ids)
*/
int board_init(void)
{
+ /* Do clocks and UART first so that printf() works */
clock_init();
clock_verify();
+#ifdef CONFIG_SPI_UART_SWITCH
+ gpio_config_uart();
+#endif
#ifdef CONFIG_TEGRA2_SPI
spi_init();
#endif
@@ -152,7 +156,11 @@ int board_early_init_f(void)
pin_mux_uart(uart_ids);
/* Initialize periph GPIOs */
+#ifdef CONFIG_SPI_UART_SWITCH
+ gpio_early_init_uart();
+#else
gpio_config_uart();
+#endif
return 0;
}
#endif /* EARLY_INIT */
diff --git a/board/nvidia/common/board.h b/board/nvidia/common/board.h
index 1f57086602..80fdcbe07a 100644
--- a/board/nvidia/common/board.h
+++ b/board/nvidia/common/board.h
@@ -26,5 +26,6 @@
void gpio_config_uart(void);
int tegra2_mmc_init(int dev_index, int bus_width, int pwr_gpio, int cd_gpio);
+void gpio_early_init_uart(void);
#endif /* BOARD_H */
diff --git a/board/nvidia/seaboard/seaboard.c b/board/nvidia/seaboard/seaboard.c
index 7f2827b8be..0b779f6e9e 100644
--- a/board/nvidia/seaboard/seaboard.c
+++ b/board/nvidia/seaboard/seaboard.c
@@ -31,6 +31,8 @@
#endif
#include "../common/board.h"
+/* TODO: Remove this code when the SPI switch is working */
+#ifndef CONFIG_SPI_UART_SWITCH
/*
* Routine: gpio_config_uart_seaboard
* Description: Force GPIO_PI3 low on Seaboard so UART4 works.
@@ -48,6 +50,7 @@ void gpio_config_uart(void)
return;
gpio_config_uart_seaboard();
}
+#endif
#ifdef CONFIG_TEGRA2_MMC
/*
OpenPOWER on IntegriCloud