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authorUwe Kleine-König <u.kleine-koenig@pengutronix.de>2013-06-28 11:49:41 +0200
committerGreg Kroah-Hartman <gregkh@linuxfoundation.org>2013-07-26 16:34:00 -0700
commit079a036f4283e2b0e5c26080b8c5112bc0cc1831 (patch)
tree0e4e39b000d63c5a49d37b06f101d0f237fee73f /drivers/tty/serial/mxs-auart.c
parentd970d7fe65adff5efe75b4a73c4ffc9be57089f7 (diff)
downloadtalos-obmc-linux-079a036f4283e2b0e5c26080b8c5112bc0cc1831.tar.gz
talos-obmc-linux-079a036f4283e2b0e5c26080b8c5112bc0cc1831.zip
serial/mxs-auart: increase time to wait for transmitter to become idle
Without this patch the driver waits ~1 ms for the UART to become idle. At 115200n8 this time is (theoretically) enough to transfer 11.5 characters (= 115200 bits/s / (10 Bits/char) * 1ms). As the mxs-auart has a fifo size of 16 characters the clock is gated too early. The problem is worse for lower baud rates. This only happens to really shut down the transmitter in the middle of a transfer if /dev/ttyAPPx isn't opened in userspace (e.g. by a getty) but was at least once (because the bootloader doesn't disable the transmitter). So increase the timeout to 20 ms which should be enough for 9600n8, too. Moreover skip gating the clock if the timeout is elapsed. Cc: stable@vger.kernel.org # v2.6.39+ Signed-off-by: Uwe Kleine-König <u.kleine-koenig@pengutronix.de> Signed-off-by: Greg Kroah-Hartman <gregkh@linuxfoundation.org>
Diffstat (limited to 'drivers/tty/serial/mxs-auart.c')
-rw-r--r--drivers/tty/serial/mxs-auart.c21
1 files changed, 13 insertions, 8 deletions
diff --git a/drivers/tty/serial/mxs-auart.c b/drivers/tty/serial/mxs-auart.c
index 3de0fb2712f5..f85b8e6d0346 100644
--- a/drivers/tty/serial/mxs-auart.c
+++ b/drivers/tty/serial/mxs-auart.c
@@ -851,7 +851,7 @@ auart_console_write(struct console *co, const char *str, unsigned int count)
struct mxs_auart_port *s;
struct uart_port *port;
unsigned int old_ctrl0, old_ctrl2;
- unsigned int to = 1000;
+ unsigned int to = 20000;
if (co->index >= MXS_AUART_PORTS || co->index < 0)
return;
@@ -872,18 +872,23 @@ auart_console_write(struct console *co, const char *str, unsigned int count)
uart_console_write(port, str, count, mxs_auart_console_putchar);
- /*
- * Finally, wait for transmitter to become empty
- * and restore the TCR
- */
+ /* Finally, wait for transmitter to become empty ... */
while (readl(port->membase + AUART_STAT) & AUART_STAT_BUSY) {
+ udelay(1);
if (!to--)
break;
- udelay(1);
}
- writel(old_ctrl0, port->membase + AUART_CTRL0);
- writel(old_ctrl2, port->membase + AUART_CTRL2);
+ /*
+ * ... and restore the TCR if we waited long enough for the transmitter
+ * to be idle. This might keep the transmitter enabled although it is
+ * unused, but that is better than to disable it while it is still
+ * transmitting.
+ */
+ if (!(readl(port->membase + AUART_STAT) & AUART_STAT_BUSY)) {
+ writel(old_ctrl0, port->membase + AUART_CTRL0);
+ writel(old_ctrl2, port->membase + AUART_CTRL2);
+ }
clk_disable(s->clk);
}
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