| Commit message (Collapse) | Author | Age | Files | Lines |
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Systems with unmaskable interrupts such as SMIs may massively
underestimate loops_per_jiffy, and fail to converge anywhere near the real
value. A case seen on x86_64 was an initial estimate of 256<<12, which
converged to 511<<12 where the real value should have been over 630<<12.
This admitedly requires bypassing the TSC calibration (lpj_fine), and a
failure to settle in the direct calibration too, but is physically
possible. This failure does not depend on my previous calibration
optimisation, but by luck is easy to fix with the optimisation in place
with a trivial retry loop.
In the context of the optimised converging method, as we can no longer
trust the starting estimate, enlarge the search bounds exponentially so
that the number of retries is logarithmically bounded.
[akpm@linux-foundation.org: mention x86_64 SMIs in comment]
Signed-off-by: Phil Carmody <ext-phil.2.carmody@nokia.com>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: "H. Peter Anvin" <hpa@zytor.com>
Tested-by: Stephen Boyd <sboyd@codeaurora.org>
Cc: Greg KH <greg@kroah.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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Binary chop with a jiffy-resync on each step to find an upper bound is
slow, so just race in a tight-ish loop to find an underestimate.
If done with lots of individual steps, sometimes several hundreds of
iterations would be required, which would impose a significant overhead,
and make the initial estimate very low. By taking slowly increasing steps
there will be less overhead.
E.g. an x86_64 2.67GHz could have fitted in 613 individual small delays,
but in reality should have been able to fit in a single delay 644 times
longer, so underestimated by 31 steps. To reach the equivalent of 644
small delays with the accelerating scheme now requires about 130
iterations, so has <1/4th of the overhead, and can therefore be expected
to underestimate by only 7 steps.
As now we have a better initial estimate we can binary chop over a smaller
range. With the loop overhead in the initial estimate kept low, and the
step sizes moderate, we won't have under-estimated by much, so chose as
tight a range as we can.
Signed-off-by: Phil Carmody <ext-phil.2.carmody@nokia.com>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: "H. Peter Anvin" <hpa@zytor.com>
Tested-by: Stephen Boyd <sboyd@codeaurora.org>
Cc: Greg KH <greg@kroah.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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The motivation for this patch series is that currently our OMAP calibrates
itself using the trial-and-error binary chop fallback that some other
architectures no longer need to perform. This is a lengthy process,
taking 0.2s in an environment where boot time is of great interest.
Patch 2/4 has two optimisations. Firstly, it replaces the initial
repeated- doubling to find the relevant power of 2 with a tight loop that
just does as much as it can in a jiffy. Secondly, it doesn't binary chop
over an entire power of 2 range, it choses a much smaller range based on
how much it squeezed in, and failed to squeeze in, during the first stage.
Both are significant optimisations, and bring our calibration down from
23 jiffies to 5, and, in the process, often arrive at a more accurate lpj
value.
The 'bands' and 'sub-logarithmic' growth may look over-engineered, but
they only cost a small level of inaccuracy in the initial guess (for all
architectures) in order to avoid the very large inaccuracies that appeared
during testing (on x86_64 architectures, and presumably others with less
metronomic operation). Note that due to the existence of the TSC and
other timers, the x86_64 will not typically use this fallback routine, but
I wanted to code defensively, able to cope with all kinds of processor
behaviours and kernel command line options.
Patch 3/4 is an additional trap for the nightmare scenario where the
initial estimate is very inaccurate, possibly due to things like SMIs.
It simply retries with a larger bound.
Stephen said:
I tried this patch set out on an MSM7630.
:
: Before:
:
: Calibrating delay loop... 681.57 BogoMIPS (lpj=3407872)
:
: After:
:
: Calibrating delay loop... 680.75 BogoMIPS (lpj=3403776)
:
: But the really good news is calibration time dropped from ~247ms to ~56ms.
: Sadly we won't be able to benefit from this should my udelay patches make
: it into ARM because we would be using calibrate_delay_direct() instead (at
: least on machines who choose to). Can we somehow reapply the logic behind
: this to calibrate_delay_direct()? That would be even better, but this is
: definitely a boot time improvement.
:
: Or maybe we could just replace calibrate_delay_direct() with this fallback
: calculation? If __delay() is a thin wrapper around read_current_timer()
: it should work just as well (plus patch 3 makes it handle SMIs). I'll try
: that out.
This patch:
... so that it can be modified more clinically.
This is almost entirely cosmetic. The only change to the operation
is that the global variable is only set once after the estimation is
completed, rather than taking on all the intermediate values. However,
there are no readers of that variable, so this change is unimportant.
Signed-off-by: Phil Carmody <ext-phil.2.carmody@nokia.com>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: "H. Peter Anvin" <hpa@zytor.com>
Tested-by: Stephen Boyd <sboyd@codeaurora.org>
Cc: Greg KH <greg@kroah.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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Fixes a hang when booting as dom0 under Xen, when jiffies can be
quite large by the time the kernel init gets this far.
Signed-off-by: Tim Deegan <Tim.Deegan@citrix.com>
[jbeulich@novell.com: !time_after() -> time_before_eq() as suggested by Jiri Slaby]
Signed-off-by: Jan Beulich <jbeulich@novell.com>
Cc: Jiri Slaby <jslaby@suse.cz>
Cc: Jeremy Fitzhardinge <jeremy@goop.org>
Cc: stable@kernel.org
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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Limit the number of per cpu calibration messages by only
printing out results for the first cpu to boot.
Also, don't print "CPUx is down" as this is expected, and we
don't need 4096 reminders... ;-)
Signed-off-by: Mike Travis <travis@sgi.com>
Cc: Heiko Carstens <heiko.carstens@de.ibm.com>
Cc: Roland Dreier <rdreier@cisco.com>
Cc: Randy Dunlap <rdunlap@xenotime.net>
Cc: Tejun Heo <tj@kernel.org>
Cc: Andi Kleen <andi@firstfloor.org>
Cc: Greg Kroah-Hartman <gregkh@suse.de>
Cc: Yinghai Lu <yhlu.kernel@gmail.com>
Cc: David Rientjes <rientjes@google.com>
Cc: Steven Rostedt <rostedt@goodmis.org>
Cc: Rusty Russell <rusty@rustcorp.com.au>
Cc: Hidetoshi Seto <seto.hidetoshi@jp.fujitsu.com>
Cc: Jack Steiner <steiner@sgi.com>
Cc: Frederic Weisbecker <fweisbec@gmail.com>
LKML-Reference: <20091118002219.889552000@alcatraz.americas.sgi.com>
Signed-off-by: Ingo Molnar <mingo@elte.hu>
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Rabin Vincent noticed that there's a stray <6> in BogoMIPS printk:
> Remove the extra KERN_INFO which causes this:
> Calibrating delay loop... <6>179.40 BogoMIPS (lpj=897024)
> - printk(KERN_INFO "%lu.%02lu BogoMIPS (lpj=%lu)\n",
> - loops_per_jiffy/(500000/HZ),
> - (loops_per_jiffy/(5000/HZ)) % 100, loops_per_jiffy);
> + printk("%lu.%02lu BogoMIPS (lpj=%lu)\n",
> + loops_per_jiffy/(500000/HZ),
> + (loops_per_jiffy/(5000/HZ)) % 100, loops_per_jiffy);
> }
How about just using KERN_CONT and leaving the whitespace
for a patch that does the entire file?
Reported-by: Rabin Vincent <rabin@rab.in>
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As suggested by Ingo, remove all references to tsc from init/calibrate.c
TSC is x86 specific, and using tsc in variable names in a generic file should
be avoided. lpj_tsc is now called lpj_fine, since it is related to fine tuning
of lpj value. Also tsc_rate_* is called timer_rate_*
Signed-off-by: Alok N Kataria <akataria@vmware.com>
Cc: Arjan van de Ven <arjan@infradead.org>
Cc: Daniel Hecht <dhecht@vmware.com>
Cc: Tim Mann <mann@vmware.com>
Cc: Zach Amsden <zach@vmware.com>
Cc: Sahil Rihan <srihan@vmware.com>
Signed-off-by: Ingo Molnar <mingo@elte.hu>
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On the x86 platform we can use the value of tsc_khz computed during tsc
calibration to calculate the loops_per_jiffy value. Its very important
to keep the error in lpj values to minimum as any error in that may
result in kernel panic in check_timer. In virtualization environment, On
a highly overloaded host the guest delay calibration may sometimes
result in errors beyond the ~50% that timer_irq_works can handle,
resulting in the guest panicking.
Does some formating changes to lpj_setup code to now have a single
printk to print the bogomips value.
We do this only for the boot processor because the AP's can have
different base frequencies or the BIOS might boot a AP at a different
frequency.
Signed-off-by: Alok N Kataria <akataria@vmware.com>
Cc: Arjan van de Ven <arjan@infradead.org>
Cc: Daniel Hecht <dhecht@vmware.com>
Cc: Tim Mann <mann@vmware.com>
Cc: Zach Amsden <zach@vmware.com>
Cc: Sahil Rihan <srihan@vmware.com>
Signed-off-by: Ingo Molnar <mingo@elte.hu>
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calibrate_delay() must be __cpuinit, not __{dev,}init.
I've verified that this is correct for all users.
While doing the latter, I also did the following cleanups:
- remove pointless additional prototypes in C files
- ensure all users #include <linux/delay.h>
This fixes the following section mismatches with CONFIG_HOTPLUG=n,
CONFIG_HOTPLUG_CPU=y:
WARNING: vmlinux.o(.text+0x1128d): Section mismatch: reference to .init.text.1:calibrate_delay (between 'check_cx686_slop' and 'set_cx86_reorder')
WARNING: vmlinux.o(.text+0x25102): Section mismatch: reference to .init.text.1:calibrate_delay (between 'smp_callin' and 'cpu_coregroup_map')
Signed-off-by: Adrian Bunk <bunk@kernel.org>
Cc: Ivan Kokshaysky <ink@jurassic.park.msu.ru>
Cc: Richard Henderson <rth@twiddle.net>
Cc: "Luck, Tony" <tony.luck@intel.com>
Cc: Ralf Baechle <ralf@linux-mips.org>
Cc: Paul Mackerras <paulus@samba.org>
Cc: Benjamin Herrenschmidt <benh@kernel.crashing.org>
Cc: "David S. Miller" <davem@davemloft.net>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Christian Zankel <chris@zankel.net>
Cc: Heiko Carstens <heiko.carstens@de.ibm.com>
Cc: Martin Schwidefsky <schwidefsky@de.ibm.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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- All implementations can be __devinit
- The function prototypes were in asm/timex.h but they all must be the same,
so create a single declaration in linux/timex.h.
- uninline the sparc64 version to match the other architectures
- Don't bother #defining ARCH_HAS_READ_CURRENT_TIMER to a particular value.
[ezk@cs.sunysb.edu: fix build]
Cc: "David S. Miller" <davem@davemloft.net>
Cc: Haavard Skinnemoen <hskinnemoen@atmel.com>
Cc: Thomas Gleixner <tglx@linutronix.de>
Cc: Ingo Molnar <mingo@elte.hu>
Cc: Andi Kleen <ak@suse.de>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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Optionally add a boot delay after each kernel printk() call, crudely
measured in milliseconds, with a maximum delay of 10 seconds per printk.
Enable CONFIG_BOOT_PRINTK_DELAY=y and then add (e.g.):
"lpj=loops_per_jiffy boot_delay=100"
to the kernel command line.
It has been useful in cases like "during boot, my machine just reboots or the
screen goes black" by slowing down printk, (and adding initcall_debug), we can
usually see the last thing that happened before the lights went out which is
usually a valuable clue.
[akpm@linux-foundation.org: not all architectures implement CONFIG_HZ]
[akpm@linux-foundation.org: fix lots of stuff]
[bunk@stusta.de: kernel/printk.c: make 2 variables static]
[heiko.carstens@de.ibm.com: fix slow down printk on boot compile error]
Signed-off-by: Randy Dunlap <rdunlap@xenotime.net>
Signed-off-by: Dave Jones <davej@redhat.com>
Signed-off-by: Adrian Bunk <bunk@stusta.de>
Signed-off-by: Heiko Carstens <heiko.carstens@de.ibm.com>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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After Al Viro (finally) succeeded in removing the sched.h #include in module.h
recently, it makes sense again to remove other superfluous sched.h includes.
There are quite a lot of files which include it but don't actually need
anything defined in there. Presumably these includes were once needed for
macros that used to live in sched.h, but moved to other header files in the
course of cleaning it up.
To ease the pain, this time I did not fiddle with any header files and only
removed #includes from .c-files, which tend to cause less trouble.
Compile tested against 2.6.20-rc2 and 2.6.20-rc2-mm2 (with offsets) on alpha,
arm, i386, ia64, mips, powerpc, and x86_64 with allnoconfig, defconfig,
allmodconfig, and allyesconfig as well as a few randconfigs on x86_64 and all
configs in arch/arm/configs on arm. I also checked that no new warnings were
introduced by the patch (actually, some warnings are removed that were emitted
by unnecessarily included header files).
Signed-off-by: Tim Schmielau <tim@physik3.uni-rostock.de>
Acked-by: Russell King <rmk+kernel@arm.linux.org.uk>
Signed-off-by: Andrew Morton <akpm@linux-foundation.org>
Signed-off-by: Linus Torvalds <torvalds@linux-foundation.org>
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Issue:
Current tsc based delay_calibration can result in significant errors in
loops_per_jiffy count when the platform events like SMIs
(System Management Interrupts that are non-maskable) are present. This could
lead to potential kernel panic(). This issue is becoming more visible with 2.6
kernel (as default HZ is 1000) and on platforms with higher SMI handling
latencies. During the boot time, SMIs are mostly used by BIOS (for things
like legacy keyboard emulation).
Description:
The psuedocode for current delay calibration with tsc based delay looks like
(0) Estimate a value for loops_per_jiffy
(1) While (loops_per_jiffy estimate is accurate enough)
(2) wait for jiffy transition (jiffy1)
(3) Note down current tsc (tsc1)
(4) loop until tsc becomes tsc1 + loops_per_jiffy
(5) check whether jiffy changed since jiffy1 or not and refine
loops_per_jiffy estimate
Consider the following cases
Case 1:
If SMIs happen between (2) and (3) above, we can end up with a
loops_per_jiffy value that is too low. This results in shorted delays and
kernel can panic () during boot (Mostly at IOAPIC timer initialization
timer_irq_works() as we don't have enough timer interrupts in a specified
interval).
Case 2:
If SMIs happen between (3) and (4) above, then we can end up with a
loops_per_jiffy value that is too high. And with current i386 code, too
high lpj value (greater than 17M) can result in a overflow in
delay.c:__const_udelay() again resulting in shorter delay and panic().
Solution:
The patch below makes the calibration routine aware of asynchronous events
like SMIs. We increase the delay calibration time and also identify any
significant errors (greater than 12.5%) in the calibration and notify it to
user.
Patch below changes both i386 and x86-64 architectures to use this
new and improved calibrate_delay_direct() routine.
Signed-off-by: Venkatesh Pallipadi <venkatesh.pallipadi@intel.com>
Signed-off-by: Adrian Bunk <bunk@stusta.de>
Signed-off-by: Andrew Morton <akpm@osdl.org>
Signed-off-by: Linus Torvalds <torvalds@osdl.org>
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Initial git repository build. I'm not bothering with the full history,
even though we have it. We can create a separate "historical" git
archive of that later if we want to, and in the meantime it's about
3.2GB when imported into git - space that would just make the early
git days unnecessarily complicated, when we don't have a lot of good
infrastructure for it.
Let it rip!
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