diff options
author | Russell King <rmk+kernel@arm.linux.org.uk> | 2012-01-21 18:24:17 +0000 |
---|---|---|
committer | Russell King <rmk+kernel@arm.linux.org.uk> | 2012-02-18 23:15:41 +0000 |
commit | 2b4d9d2b001be2ff06be2ea5c52e9adaf85b0805 (patch) | |
tree | 1f20cf005a8f9e47a11464f3012a822557e2f041 | |
parent | ed442b6798eb39eda3bcea92ef9403280b603818 (diff) | |
download | blackbird-op-linux-2b4d9d2b001be2ff06be2ea5c52e9adaf85b0805.tar.gz blackbird-op-linux-2b4d9d2b001be2ff06be2ea5c52e9adaf85b0805.zip |
MFD: ucb1x00-core: disable mcp clock when bus is not required
The ucb1x00-core was leaving the mcp clock enabled indefinitely after
probe. This needlessly wastes power. Add the necessary disables to
ensure that the clock remains off when we don't need it.
Acked-by: Jochen Friedrich <jochen@scram.de>
Signed-off-by: Russell King <rmk+kernel@arm.linux.org.uk>
-rw-r--r-- | drivers/mfd/ucb1x00-core.c | 9 |
1 files changed, 5 insertions, 4 deletions
diff --git a/drivers/mfd/ucb1x00-core.c b/drivers/mfd/ucb1x00-core.c index 9f8ea52f0ca8..ed2a4b2e518f 100644 --- a/drivers/mfd/ucb1x00-core.c +++ b/drivers/mfd/ucb1x00-core.c @@ -554,16 +554,17 @@ static int ucb1x00_probe(struct mcp *mcp) mcp_enable(mcp); id = mcp_reg_read(mcp, UCB_ID); + mcp_disable(mcp); if (id != UCB_ID_1200 && id != UCB_ID_1300 && id != UCB_ID_TC35143) { printk(KERN_WARNING "UCB1x00 ID not found: %04x\n", id); - goto err_disable; + goto out; } ucb = kzalloc(sizeof(struct ucb1x00), GFP_KERNEL); ret = -ENOMEM; if (!ucb) - goto err_disable; + goto out; device_initialize(&ucb->dev); ucb->dev.class = &ucb1x00_class; @@ -581,7 +582,9 @@ static int ucb1x00_probe(struct mcp *mcp) if (ret) goto err_dev_add; + ucb1x00_enable(ucb); ucb->irq = ucb1x00_detect_irq(ucb); + ucb1x00_disable(ucb); if (ucb->irq == NO_IRQ) { dev_err(&ucb->dev, "IRQ probe failed\n"); ret = -ENODEV; @@ -633,8 +636,6 @@ static int ucb1x00_probe(struct mcp *mcp) device_del(&ucb->dev); err_dev_add: put_device(&ucb->dev); - err_disable: - mcp_disable(mcp); out: if (pdata && pdata->reset) pdata->reset(UCB_RST_PROBE_FAIL); |